Dynamic Leadership. Unparalleled Quality.

Delivering excellence for our clients in every project.

At Evans Industrial Inc., we look at every client project as a true partnership. We understand the immense value our clients bring to our society, and take pride and ownership in every opportunity to collaborate in creating meaningful work.

Our revolutionary engineering, progressive leadership, expert team and dedication to quality is how we continuously deliver exceptional results for our clients.

We are also committed to providing cost-effective solutions for our clients and formulating efficient construction methods to deliver projects ahead of schedule whenever possible.


FEATURED PROJECTS

Power Generation Facility - Steam Valve Replacement

Evans Industrial was contracted by a Power Generation Facility to replace 7 Main Stream Valves. Our dynamic team of skilled workers used innovative construction solutions to overcome technical obstacles which resulted in significant cost reduction and project length for our client.

power generation Valve replacement.jpg

Power Generation Facility

  • Replaced 7 Main Steam Valves in two weeks working two shifts

  • Valve body material: ASTM A217

  • Piping material: ASTM P91, Inlet 16” Schedule 160, Outlet 12” Schedule 160

  • 100% Weld Acceptance

The unique location of the valves in the unit posed a logistical challenge for workers to access and would typically require a 250 ton crane. Commissioning this equipment would be the easiest solution, but would add significant cost to the project. 

Leveraging our team’s ingenuity, we delivered a cost-effective solution by designing and installing temporary monorails above the valve. This provided direct rigging access to the valves without the added expense of a crane and resulted in significant cost savings for our client. 

Our team was also able to cut weld inspection time of the project. The 9-chrome material used required a 14 hour stress relief cycle. Understanding this delay within the project scope, our expert welders and quality control personnel created a more efficient process to complete the project. Rather than waiting between heat cycles to perform the varied tasks, our team worked within the heat cycles which enabled the completion of both welding and stress relief in conjunction. This process allowed immediate inspections of welds, all passing 100% X-Ray acceptance, saving 12 hours per weld on project time. 


Combined-Cycle Power Plant - Hot Gas Piping Replacement

When a leading Water and Power Generation facility contracted Evans Industrial to replace their hot gas piping, we implemented comprehensive project management and productive scheduling to deliver project results with safety, quality and efficiency. 

Combined-Cycle Power Plant stainless steel piping

Combined-Cycle Power Plant

• Replaced hot gas path stainless steel piping in 4 units

• 90 welds, 316 stainless steel sizes 8” to 4”

• Install stainless steel tubing for instrumentation 1,000 linear feet

• Passivation of stainless steel field welded components

• 10% X-Ray, 100% Acceptance

• Submitted R1 form and quality control package following

completion of the project.

The project required simultaneous replacement of hot gas piping in four turbines. Leveraging a thorough planning process, we created an effective working schedule for each of the four turbines independent of one another.

Utilizing Primavera P6, we developed a robust, detailed schedule load of man-hours dedicated to each task. We reviewed this scheduling track every 24 hours to identify recourse potential roadblocks and optimize the acceleration of the project.

Our scheduling management further increased productivity for the project by allowing us to share resources among the units.  We assembled four crews of highly skilled workers who were able to safely remove the existing piping and install new piping with proficiency. Each crew featured dedicated quality control personnel to ensure impressive service standards were met during construction. All welds were passed 100% X-Ray acceptance.


Southern California Water District
UV Reactor Water Treatment Facility

When a Southern California Water District planned to upgrade their facility with an Ultraviolet Light Advanced Oxidation Treatment System, they turned to Evans Industrial Inc. as a trusted construction partner and strategic project management resource.  

UV Reactor Water Treatment Facility Construction, general contractor, welding, pipe fitting, ASME "R" stamp, pipe line repair & installation, pump station repair & installation
Construction, general contractor, welding, pipe fitting, ASME "R" stamp, pipe line repair & installation, pump station repair & installation, Water district

The project initiative involved rigging the new, 8,000 pound equipment into their existing warehouse. The project posed logistical challenges as the existing warehouse roll-up doors were only 12 feet tall, but our team was highly capable in delivering results. We constructed a comprehensive rigging plan utilizing high load carrying roller bearings, that allowed seamless transportation of the new equipment through the doors and in position.

Our team strategically coordinated the retrofitting of our client’s existing warehouse into a UV Reactor Treatment Facility through the installation of the outside pipeline.

Construction, general contractor, welding, pipe fitting, ASME "R" stamp, pipe line repair & installation, pump station repair & installation

Using Primavera P6, we developed a comprehensive, man-hour loaded schedule that was reviewed and modified daily for optimal productivity. Our project dedication and consistent daily involvement made it possible for us to easily identify creative opportunities to shift resources during the construction and save time.

Since the Ultraviolet water purification system was a new technology for our client, we commissioned the equipment suppliers’ technical staff at various stages during construction. This involvement generated transparent communication during construction and provided the ability to quickly identify and correct process challenges during this phase.

Taking the extra steps in commissioning the suppliers’ technical support resulted in a flawless finished product. Once the Ultraviolet water purification system came on the line, the equipment produced the product on specification immediately after start up.

Construction, general contractor, welding, pipe fitting, ASME "R" stamp, pipe line repair & installation, pump station repair & installation - water district